Why is pitch and roll swapped on betaflight
I am losing my mind from this darwinfpv f405 stack, was just about to hover test the drone but it kept flipping out. Checked the setup 3d model and just realized this. I have been trying to figure it out since morning and it still won't budge, I've tried changing board orientation and checking board arrow but no change. Does any of you ever have this same problem or maybe have a fix?