Throttle “Stuck” and can’t figure it out.
*I TRIED THIS WITOUT HOLDING IT ASWELL DOES SAME THING, JUST HELD IT BECAUSE I CANT RECORD ME FLYING EASILY
So just bought another new air75 and when I set it up and tried to fly it it was flipping over instantly and saying runaway so I went into beta flight and the flight controller was all wack in the 3D model so I adjust that so the 3D model accurately represents how my drone is oriented. But still like the video shows I arm it motors start normally then when I throttle up and back down it just keeps going up and only stops when I disarm it so I had to catch it out of the sky. It doesn’t spin or do anything other than shoot up.
Here’s some things I’ve already tried/looked at
- Checked the motor and propeller direction physically and on betaflight. My motors are set as reversed because of propeller direction.
- checked to make sure the receiver throttle in betaflight was acting correctly, going from 1000 up and then back down to 1000.
- adjusted the 3D model, had to adjust alignment with the yaw setting to 225 for it to act correctly.
Please help this is super annoying and have tried and watched many videos. Feel free to ask any more about what I’ve done as I may have missed things I’ve tried. Thank you!!